danhampson
Member
ive converted my protos to fbl with msh brain as fbl controller and got a hobbywing rpm sensor to set up the governor,edive changed the plug on the sensor ensuring that the polarity is correct and soldered the pickup wires to the motor.
ive activated the governor on bank 1 for testing, and changed the sensing divisor to 5 (half the pole count of the motor).
When the brain is plugged into the computer the magnet detected box isnt checked when the head is turned and there isnt any readout for the head rpm.
the sensor is getting very hot.
ive activated the governor on bank 1 for testing, and changed the sensing divisor to 5 (half the pole count of the motor).
When the brain is plugged into the computer the magnet detected box isnt checked when the head is turned and there isnt any readout for the head rpm.
the sensor is getting very hot.
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